

Engine (40%)
Transmission and Drivetrain (13%)
Brakes and Traction Control (4%)
Suspension and Steering (10%)
Electrical and Air Conditioning (30%)
Paint, Rust, Leaks, Rattles, and Trim (2%)
Other (2%)
$2500+ (2%)
$1000 - $2499 (13%)
$500 - $999 (9%)
$100 - $499 (36%)
< $100 (40%)
Engine not specified
117800 mi R 7000 |
The no 4 injector was totally damaged and could not be repaired and had to be replaced this was after rust was found in the diesel pump |
turbocharged 138hp 2.5L I4 Diesel 5-speed manual 4WD, part-time w/low range
108500 mi R 500 |
Replaced heater core inder dash. |
44000 mi £343 |
Blocked fuel system and fuel pump. Fuel pump removes and cleaned, fuel lines flushed, fuel filter replaced. |
turbocharged 138hp 2.5L I4 Diesel 5-speed automatic 4WD, part-time w/low range
107000 mi £80 |
replaced idler pulley of aux belt. installed super locker mod to override the tod system if needed. |
73460 mi $400 |
Knocking engine noise on the timing chain cover. Replaced timing chain, chain tensioner and timing chain guide. |
110360 mi €600 |
New clutch assembly installed, due to slipping clutch. |
79980 mi R 88 |
Replace top radiator hose after hose split Replace top radiator hose after hose split |
119020 mi R 20 |
Replace leaking water hoses Replaced worn turbocharger Replaced worn turbocharger Replace leaking water hoses |
143600 mi R 250 |
Fuel tank lining disintegrated and clogged diesel filter causing power loss and engine check light. Tank inside stripped, cleaned and flushed. Fuel lines flushed and filters replaced. |
157480 mi R 160 |
EGR valve sticking open causing black smoke and power loss. Inlet manifold removed and cleaned, blanking plate fitted to EGR pipe. |
171120 mi R 200 |
4 broken studs on exhaust manifold. All studs and nuts replaced. |
173600 mi R 15 |
Top radiator hose leaking, replaced |
192-horsepower 3.5L V6 5-speed manual 4WD, part-time w/low range
89000 mi US $550 |
replaced radiator |
101000 mi US $75 |
radiator reservoir cracked, replaced |
105000 mi US $1528 |
bad water pump, also replaced timing belt |
105000 mi | engine skipping, cam tensioners worn, replaced at no charge |
192-horsepower 3.5L V6 5-speed automatic RWD
132000 mi US $120 |
It would start to overheat, shut down and I found that the nipple on top of radiator was broke off and had a screw inserted,the hose was also plugged, the y on back of eng.was melted,no water,replaced radiator,Y and a few lines and it's ok. |
140000 mi US $1350 |
Radiator hoses needed replacement along with water pump. Plus oil system needed help. Old age. |
127000 mi US $250 |
Replacement of head gasket and seals for oil leakage. Replacement of spark plugs. |
47000 mi US $200 |
Accelerator cable was fraying inside its sheath, causing erratic pedal movement. |
48000 mi US $10 |
throttle plate carbon deposits. Dealer claimed to clean and lubricate. |
192-horsepower 3.5L V6 5-speed automatic AWD w/low range
80000 mi US $40 |
Replaced lower radiator hose |
97000 mi US $200 |
crank sprocket replaced. Overheating/Replaced reservoir. Seam on orig reservoir separated. Overheating: Could not locate problem Overheating/Replaced hose clamps. Overheating/Replaced water pump. |
97000 mi | Overheated now wont start. Can't locate problem. Car has been sitting for a month after having continued overheating, replaced all possible problematic parts w/o resolution. Won't start post water pump. |
76880 mi R 300 |
Crankshaft bolt came loose 1800 km after major service was done. Cause:Old crankshaft bolt was re-used although the procedure states that bolt must be replaced when removed!! |
192-horsepower 3.5L V6 5-speed automatic 4WD, part-time w/low range
127000 mi US $215 |
Replaced both flex pipes in the exhaust. Removed and welded in new flex pipes. |
139000 mi US $800 |
Check Engine Light. Purge valve needed replaced. Leaking hose in vapor recovery system repaired |
160800 mi US $2100 |
Leak in the gas tank at a seam |
197600 mi US $240 |
Coolant leaking from hose at rear of engine compartment |
211500 mi US $160 |
Radiator and upper hose replaced |
80000 mi US $2 |
Crankshaft pulley bolt, broke in half, caused a lot of damage water pump, and so on. KIA should recall this part as it as happens a lot to Kia Sorento, all years it cost me $1474 to fix this mess,for a $ 10.00 part. |
109740 mi C $45 |
Replaced the tensioner pulley for the alternator belt (was beginning to make a squealing sound) |
90200 mi US $2200 |
Loss of coolant due to bad design of system. New heads, pistons, bearings,r&r of block, new timing belt, bolt. New temp sensors. Water coolant line failed at tank. Sensor not able to measure temp due to poor design location. |
91000 mi | Crankcase sensor failed. Purchased new to be installed shortly. |
91500 mi | ECM & eng fuse relay box replaced. AC/ high switch causing blown fuses in INJ fuse. Issue is endemic to kia sorento 2003-2006 shows DTC CODE OF crankcase sensor. ECM CONTINUES TO EXHIBIT UNUSUAL SIDE EFFECTS AFTER ENG ISSUE AS NOTED IN PAST Parts replaced. ECM and Fuse relay |
turbocharged 4-cylinder diesel automatic 4WD
79600 mi | ok was diagnosed with tank delamination! replaced tank cleaned fuel lines replaced fuel filter after replacing tank the car then kept stalling again and became hard to start. they checked for injector problems and changed only one injector! they kept it for over a month but now it doesn't start. will try a diesel specialist to get it fixed. |
81000 mi £250 |
turns out i had a faulty injector dump valve this was my fault!! the kia garage had the car 1.5 months and couldnt sort this out!! these specialists did the job in one day back on the road better than ever! |